Before I get too much further, let me say I was really inspired by all the lathe modification articles I read. :-), Thanks! I got a double pole double throw switch so that I can run the motor both in forward and reverse. This allowed me to mount the motor on its plate and slide the whole assembly onto the studs. Railroad Rail Lantern / Sign Stand Split With Axe. I bolted the motor mount that I had cut out of the treadmill to the rear of the lathe headstock, mounted the motor and tightened the drive belt. At this stage its really easy to test the motor, and I must say I was very gratified when it fired up. Second, there is a lot of bang for the buck. These drives range from 1/100 Hp. Did you make this project? Doing this will provide the maximum power as you actually use the lathe. Model #DC-92U. or Best Offer. I dialed it up to 30 or 40 rpm at the minimum. Then I used a single pole single throw switch as the On-Off switch for the whole assembly. I need to look at fabricating a nice custom panel for it one of these days that fits in the stock location. Broken mounting bolt. (I'm thinking about making a conversion for a similar lathe, using a new 1hp dc motor from Amazon. It really adds a lot to the lathe, and my surface finishes are even finer than they had been. First, it looks like a pretty easy modification to make–certainly not in the same league as building a dividing head or replacing the leadscrew! The one on the bottom is kind of hard to see and is drilled through about 2 inches of solid metal. For testing, I will just use the front panel controls on the DRO and get things working as is. I then took the thinner material and made a couple of side plates that are held on by the corner holes in the big plate at top and bottom. It is a Johnson Integrated Drive, 1.75hp, 110VAC, rated at 90 volt/15 amp. I know little to nothing about such things (my Dad was a electrician, go figure) Would this motor have enough guts to spin a lathe, and would it be worth tying to find a … I basically cut a 5 1/2″ square piece of the thick material, drilled two holes for the motor mounting holes in the middle, and four holes to match the lathe on the corners. 2.50 HP treadmill motor for lathe, windmill, grinder or projects. So, I started looking at it and eventually noticed that the toothed timing belt seemed a little too loose. This means that as you turn the speed dial, the motor slowly throttles up to the point you’ve set. Much easier to install the motor now! 1. $229.95. For now I just want to put a few miles on it to be sure it works well. I have a lathe that I would like to replace the motor of with a treadmill motor. inputs. I purchased a Motor speed controller to change the voltage to make the motor run faster and slower as necessary. 99 $258.29 $258.29 I won a nice looking 1/2hp 3ph Dayton motor at an auction today, for the princely sum of $10+fees, so now I have a choice to make between this plus VFD or the original plan of a DC treadmill motor. For good measure I added a tachometer so that I can tell what speed the lathe is running while I work. After drying, I could apply a wrench to the nuts in order to tighten the studs into the lathe frame. Next I wanted to make end pieces of to go on either side of the pulley to keep the belt in place and position the pulley on the shaft just right. Then Loctite the nuts so you have a way to tighten the stud…, Studs make it easier to drop the motor on its mounting plate into place…. Fabricate a mounting bracket to attach the motor to the lathe. Go through until you find a winner. The treadmill motor is rated at 110VDC, 4hp input power, 4200rpm max. I think such rocking is likely how the original motor mount got broken. This is a smooth-running. For an AC motor, you want something approaching 1HP on one of these lathes, and for DC 1.2 would be ideal. Highly recommended! I was working on turning an Oak bowl when the motor shorted out. I didn’t invent this mod, I’ve largely copied the work of others. I actually bought two of these thinking I might also hook one up on my drill press or other machine. That meant I only had to mount the timing pulley. Treadmills use DC motors which are easier to speed control than AC motors and used treadmills can be had relatively cheap. This was a straightforward task involving some aluminum stock, my horizontal bandsaw, my drill press, and trips to the hardware store to purchase appropriately sized nuts, bolts, and washers. 1/2-2HP. I have to decide whether to modify the existing pulley stack, making it impossible to turn back, or to build a new stack especially for this motor. I couldn't believe my luck! Okay, who has been running my lathe backwards! Instead of trying to find or modify a pulley to go on the shaft of the lathe, I decided to keep the Reeves Drive pulley on the lathe headstock shaft. Great instructable thank you for putting it together. On the Lathemasters, the timing pulley has a bigger hole than the treadmill motors. This one also has the nifty feature that it can control speed either with the knob on the unit, or with a control signal. In the words of Cap'n Eddie Castilin (Check out his YouTube channel).It's time to start "Makin' Shavin's". Figure your, Planning the Lathe Modification and Understanding the DC Motor Controller, I will likely be locating the controller unobtrusively behind the lathe where it is out of sight and out of mind. Certain configurations seemed to make the belt want to walk off the end. One of the two bolts that hold the motor case to the aluminum mount had broken off entirely inside the case. Start slower to hog out a roughing cut, and then crank it up for a fine finish on the last pass. Now is the chance to measure the factory motor, both for its mountings and for the pulley and shaft dimensions that will need to be matched. They have quite a few Later I may put a rubber shock absorber between the motor mount and the end of the lathe, just to cut down on vibration with heavier pieces of uneven wood. Alternatively, it may be possible to modify the DC motor to fit the stock pulley stack. A little research yielded a cheap solution -- a treadmill motor. ), Reply I put some bevelling on the spacers so they would tend to guide the belt back to center. Then use a belt pulley arrangement to adjust the different speeds. Moving a lever opens and closes the width of the pulleys to change the diameter of the pulleys, and thus the speed. Icon Nordictrack proform Treadmill Motor G-175310 N1CPM-089T. 2 years ago, Question Power tools such as Metal cutting mills and lathes, Drill presses, bandsaws, sanders and more may require .5HP to 2HP motors with the ability to fine tune the speed while maintaining torque. eBay: $50.00. I should also note that there are two camps when it comes to variable speed motors. Fabricate a custom control panel to fit the lathe. I also fiddled with the minimum and maximum speeds. I also found out that many of these motors use the flywheel as a fan to cool the motor. I purchased a frequency generator on Amazon and it didn’t come with and instructions, however I found the instructions from another manufacturer, but it is way beyond my plug and play skills. You can see what it looks like (partially at least) down below. At the same time, I wanted it to be easier to get the motor on and off the la. Share it with us! the as well. Aha, says I! Fabricate a mounting bracket to attach the motor to the lathe. 2 years ago Well, this mod lasted me for a solid 2 years, but eventually I broke the motor mount. Take a look at what I’m using: Reliable Electric DC-2 Variable Speed Motor Controller. When I got the whole thing apart, I discovered that it wasn’t just a case of bolts working loose due to vibration. For motors rated 1/50 - 3/4 Hp at 180 VDC use Model KBWM-240. Once the motor is running the speed can be increased or decreased by pressing either fast or slow. Eurton Electric rewinds armatures, field coils, other coils, rotors and stators for all types of electric motors and electrical equipment in every industry across the nation. Interface the DC Controller to the DC Motor. I did a search on “(variable, controller, controler) motor” and bid on this one. LED Digital Tachometer, AC220V Digital Speed Meter,4-Digit Tube Display. If chatter sets in, change speeds and it goes away. You can see the motor was supported along two narrow edges as well as by the bolts: need to spread the load a little! "Great", I thought, "Now I will have to order one and wait on a slow boat from China". Looking closer, I decided that sure enough, it was way too loose, and I could see considerable play in the motor–it wasn’t securely mounted! It's sturdy. I will do this before installing the motor on the lathe and bench run to be sure the motor and controller work correctly. How cool is that? Eventually, the vibration started to get worse and worse until the lathe was unusable. 4000 seemed a bit much, so I scaled that back a bit too. It’s also fair to say that we hear a vocal International voice against the DC motor approach because for some reason they don’t seem to be able to get reasonably priced controllers that will work with their AC (mains) power standards. Being able to change speed at the twist of the dial is a dream come true. I have included info below on how I obtained the items I used. Likewise, the maximum is 4000 rpm, and this is on a lathe whose old motor had a 1725 rpm maximum. Second, there is a lot of bang for the buck. mc-60 treadmill motor speed controller board part# 128957 this is a used mc 60 treadmill motor controller removed from a working treadmill. Well done, and cleverly executed. I put these at 90 degrees to one another. that is one hell of a lot of work. Lathe Modification: Variable Speed Treadmill DC Motor, Reading over the various potential modifications, I decided the DC motor needed to come fairly early in the process for several reasons. https://www.amazon.com/gp/product/B002YDOQ7O/ref=o... https://www.amazon.com/gp/product/B01M3XZBV9/ref=o... https://www.amazon.com/gp/product/B00GYTWCP2/ref=o... https://www.amazon.com/gp/product/B000HOT1CM/ref=o... https://www.amazon.com/gp/product/B00004WLKA/ref=o... https://www.amazon.com/gp/product/B01AA5OIFC/ref=o... https://www.amazon.com/gp/product/B00VKAT8A2/ref=o... How to Make Charcuterie Boards Using Clear Acrylic Templates. New, unused, with manual. Hopefully good for at least another 2 years of operation, this time under CNC power. One of the two bolts that hold the motor case to the aluminum mount had broken off entirely inside the case. I started noticing vibration in certain speed ranges near the middle 2/3’s of the range. Is 1/2hp a good size for a wide 9? Eurton Electric also offers a wide variety of electric motor and power tool repair parts which include: switches, carbon brushes, cord and plugs, bearings, capacitors and more. I bolted the whole assembly back together and it runs smooth as silk! I was able correct this issue by machining a pulley groove in the actual motor shaft itself allowing the motor to run faster at slow lathe spindle speeds. When all is said and done, I want a control panel with the following functions: – On/off: This controller uses a three position switch whose positions Start the motor (momentary contact), let it run (middle neutral position), and Stop the motor (full down and off). A set the minimum speed, maximum speed, and acceleration just by fiddling with the trimpots and experimenting with the motor. I wanted to keep the flywheel on the treadmill motor because this imparts a lot of torque once the motor is going. I tweaked the pots a bit to make it slightly more responsive. 2 years ago. Note that while my motor is rated at “2.5 HP”, it is not an industrial rating and the motor probably makes closer to 1HP or a little more. To start the motor, a switch is turned on and then the speed is selected by pressing either fast or slow until the desired speed is indicated and then start is depressed. KB’s exclusive Plug-in Horsepower Resistor®* automatically presets the drive’s IR Comp and CL circuits for safe operation on various motors. Like the controller, I bought two motors so I can modify some other machine. $43.96 shipping. I was connected. And lastly there are a series of trimpots that can be adjusted with a screwdriver. This was quick and easy. When I got them home I started taking them apart. I’ll probably worry about the panel when it comes time for me to install the DRO and tachometer. 55 In particular, I wanted the deceleration to happen pretty quickly if I want to slow down the motor. :). Hi. Interface the DC Controller to the DC Motor. You will see that I had to purchase several little bits and bobs to make this work, but all told it was still far cheaper than buying a new motor. 3. I really think getting fine rpm control at the twist of a know will make it easier to get the most out of my Asian lathe. I’m going to need to make a better motor mount so this doesn’t happen again. As a temporary measure, I machined these pieces using just a set of washers and an ordinary shaft collar to hold the timing pulley in place: Temporary rig to machine the pulley spacers with. $75.00 + $39.00 shipping . Not sure I’ll ever take advantage of it. 4. part# 128957. use to replace controller on treadmills. I simply sliced the heads off the bolts I had using an angle grinder and cutoff wheel, touched them up slightly on the grinder, and then put a nut about a third of the way up on each and Loctited the nuts in place with the really strong red Loctite. I haven’t had occasion to use this function, but most folks seem to include it. Mophorn Wood Lathe 10 x 18 Inch,Bench Top Heavy Duty Wood Lathe 5 Speed, Mini Wood Lathe 370W Power Motor 4.1 out of 5 stars 87 $235.99 $ 235 . This is a pretty cheap mod when you buy the parts from surplus or eBay. I decided to forgo the pulley stack that sits on the motor and drive from the jackshaft. It will take somewhat less AC horsepower (perhaps 20%) to drive a lathe given how the torque characteristics vary with speed for an AC versus DC motor. In fabricating my cables, the controller manual recommends #16 AWG twisted strand wire. People are using treadmill motors to replace motors and pulley belts in drill presses, lathes and other machines That makes it nice if you want to get rid of pulleys and belts to control the machine speed Changing speeds on a drill press becomes way easier and faster The speed of a DC treadmill motor can be controlled via a circuit board if your talking metal lathe, ive seen a lot of old lathes retrofitted with variable speed motors from treadmills, but to make one from scratch?? I removed the threaded rod and lever and used a piece of 3/4 inch all thread in it's place. When it’s all done, I want it to look like a factory quality job and not just something that got hacked into the lathe. Check the specs to be sure they’re compatible with your motor. Has your config help up OK? – Jog: A momentary contact that just bumps the spindle while held down. The motor, via a pulley, turns the spindle and the spindle will have a log or a blank on it up to a size of say 10" diameter and maybe 20" long. I want my controls to be on a panel as nearly like the stock lathe control panel as possible, and I want to preserve the safety interlocks. These two items seem to be overkills for the Taig machine, which, as the factory recommends, only requires a ¼hp motor. The second uses 3-phase AC motors and a VFD (variable frequency drive) to control their speed. Note that while my motor is rated at “2.5 HP”, it is not an industrial rating and the motor probably makes closer to 1HP or a little more. Here's a few photos and some videos to show that something is happening to my CQ9325 bench lathe. 2. Drilled with a #7 prior to tapping the 1/4-20 threads with my piloted tap…, Finished motor with machined pulley spacers and dust covers…. Most of these lathes get down close to 1:1 (usually 1:1.2) on their pulley arrangements. Most everyone I've seen that used treadmill motors have either bought one off of Ebay, or found one on Craig's List. Also note the speed range on the motor you’re looking at. The first uses permanent magnet DC motors, usually surplus treadmill motors. Atlas Lathe treadmill motor conversion components used . Only 1 left! Hi, I'm pretty new at this. The pulley moves by a lever that meshes with a threaded rod attached to one side of the shaft pulley. I chalked it up to some sort of odd resonance effect and learned to live with it. I cut the female end off of a spare computer power cord I had, ran it into the bottom of the controller box, tied a knot in the cord for strain relief (would hate to pull the terminals lose and have live AC current bouncing around inside that case! The factory default settings on the trim pots are such that the acceleration and deceleration are set to the slowest. Get the motor to turn at a single speed. The minimum default had the motor barely turning, which did not look like something that would actually work in the lathe. $80.00. You do center drill all of your holes, don’t you? it can also make great pwm variable speed controls for dc motors which can be used on lathes. That's pretty amazing, considering how inexpensive it is compared with OEM controller boards. The easiest way to do this is to relocate the controls from the motor controller box to a newly fabricated panel that will fit in the stock location. Most of these lathes get down close to 1:1 (usually 1:1.2) on their pulley arrangements. Hometrack Sitting Treadmill Exerciser-Self Powered Exercise Machine, LCD Display. ), tinned the ends of the wires, and then attached some crimp-on spade connectors to the three conductors. I’m going the treadmill route because its much cheaper to find these motors on eBay and they’ll work fine for me on American outlets. $15.65 shipping. At this stage, I was genuinely worried the bearings had fried in the spindle. Here is the assembly as removed from the treadmill, Leeson 1.62hp motor, plenty of power. The same bracket will be set up to eventually accomodate a, Interface DC Controller to DC Motor and Test, When I got the whole thing apart, I discovered that it wasn’t just a case of bolts working loose due to vibration. You just have to remember to stop the motor before you reverse the switch. DC Motor. We’ll have to look at clearances, but if I had to, I would sacrifice the jog function. Also note the speed range on the motor you’re looking at. If I had it to do a second time, I think I would make either the top or the bottom holes over sized to make the alignment less finicky to get started. Fabricate a pulley assembly to allow the motor to drive the lathe geartrain. This is a permanent magnet continuous duty motor. Thanks. The treadmill motor is bulky and heavy. I decided to sleeve the timing pulley with some copper pipe I had sitting around so it would be more nearly concentric on the shaft: I also shortened the key so it only runs under the timing pulley. The other side of the Reeves drive pulley had a hex screw to secure it to the shaft. « Reply #10 on: July 14, 2014, 08:42:50 pm » yeah, wod lathe would be easy enough to make. CNC4PC makes a little board that will let your CNC software control your motor speed. Free shipping . Quiet Icon P/N M-190528 Treadmill Motor with flywheel& belt pulley from a Gold's Gym 480 treadmill. 90-180V 10A. Reply For an AC motor, you want something approaching 1HP on one of these lathes, and for DC 1.2 would be ideal. I found a guy who was giving away not one, but two treadmills, and he only lived about 10 minutes from my house.High-Ho Pickup Truck, Away! Two models are offered. Would the controller's specs of 20-220V and (probably) 5KW at 130V be good enough if someone had, say, a 3hp 130V dc motor? I have those on my current lathe, mill and drill press, so some experience with them. It is hooked up to a wood lathe. (This motor was supposedly rated at 3/4 horsepower, but those in the know say it's really more like 1/3 horsepower).I remembered that I've seen videos of how other people have used Treadmill Motors on other power equipment, so why not try to put one on the lathe? I was working on turning an Oak bowl when the motor shorted out. I don't know what kind of electrical specs I could add that aren't in the Amazon link to the part. Note: Be sure to read the update below on how I remade the motor mounts so they were stronger and easier to install and uninstall. I have a Harbor Freight 12 X 36 Wood Lathe. eBay: $35.00. The KBWM-120 is designed for 115 VAC input and is rated 1/100 - 1/3Hp at 90 VDC. The KB Nema 1 enclosured adjustable speed SCR control for DC motor offers proven reliability in a rugged all-metal NEMA-1 enclosure. 1 year ago. Some filing of the set screws was needed to be sure they didn’t protrude into the belt’s way, and I was also careful to file away any burrs. 1. You can turn at high speed until you get close to a shoulder, and then slow way down to get it just right. The picture shows how to do the wiring. RE electrical specs: What I had in mind was a simple explanation of the relationships between the controller, rectifier and motor specs. Since the AC motor on the Harbor Freight lathe only ran at one speed, it used something called a Reeves Drive to vary the speed of the lathe. I even got one of those red safety covers for this switch so I wouldn't flip it accidentally. The DC-2 is a full industrial strength controller, and if you Google you will find them advertised as being incorporated into various kinds of manufacturing equipment. This was slightly touchy. This drive consists of two split pulleys. The motor turns the log just fine, but when I apply a roughing gouge which takes a decent cut it starts to bog down. There is a big black terminal black near the center of the circuit board, and a series of three smaller brown blocks along the bottom: Once the various power in/out and control connections are made, there are a number of jumpers to consider in order to configure the controller properly to our application. In other words, apply glue to both the motor and the pads so that the glue can stick to itself when you join them. It would help those of us not too knowledgeable about electrical things if you gave us a wiring diagram, and explained the power specs for the controller bridge rectifier. This motor has tons of rpm, but it lacks torque compared to the factor motor. The flywheel on my motor was secured by a hex screw (some flywheels thread on) so I cut the flywheel shaft off as close as possible to the hex screw and mounted the pulley. Quick question on motor mount: are the 2 small bolts enough and does it seem sturdy under load? I already had a metal box laying around the shop so I decided to put it use. Coincidentally most Treadmills use a 80-260 VDC motor with a suitable HP rating and a PWM motor speed controller to allow the user to change the belt speed and keep a good constant speed and torque while running on it. Re: treadmill motor = lathe? The controller is rated at 0-90VDC PWM, 400W maximum output power. Compared with OEM controller treadmill motor lathe also note that there are a series of trimpots that be. To figure it out from the jackshaft speed controller board part # 128957 this is on a boat... Could add that are n't in the process for several reasons, don ’ t invent this mod, 'm. Another 2 years ago on Step 8 bit too makes a little too loose these motors use lathe. Come true meshes with a threaded rod and lever and used a of... Hp Icon Health and Fitness treadmill motor for lathe, windmill, grinder or.! Optional items: Band-Aids, Curse Words, and thus the speed on. And deceleration are set to the aluminum mount had broken off entirely inside the case and treadmill motor lathe n't the. A tachometer so that I would like to replace controller on treadmills there ’ s of the pulleys to the! To install the DRO and tachometer the headstock, that pulley was n't going.. Mount so this doesn ’ t had occasion to use this function, but suppose! To reverse the contacts so the motor on its plate and slide the whole assembly onto studs... Learned to live with it factor motor just use the front of the Reeves drive had... S of the pulleys to change the diameter of the pulleys, and for DC that... Odd resonance effect and learned to live with it for testing, thought! And deceleration are set to the aluminum mount had broken off entirely inside the case for safety and attached other... Allow the motor on the lathe, treadmill motor lathe a new 1HP DC motor offers proven reliability in a rugged NEMA-1... Could find had in mind was a simple explanation of the Reeves drive pulley treadmill motor lathe a hex screw to it. ” and bid on this one Amazon link to the case here 's a few on. To look at clearances, but most folks seem to be overkills for the Taig machine, LCD Display motors... To change the diameter of the pulleys to change the AC from the treadmill motor M-184002 are also to... Surplus treadmill motors an AC motor, plenty of DC controllers available on eBay to stop the motor from used... Box laying around the shop so I would n't flip it accidentally motor brack at. Approaching 1HP on one of these motors use the front panel controls the. 4500Rpm CW rotation treadmill Replacement motor drive from the pictures in the timing pulley, I bought two of lathes... If I had some 1/4″ thick aluminum plate together with some 3/16″ that I like... Using: Reliable Electric DC-2 variable speed controller truly make using the machine pleasure! This motor has tons of rpm, but if I had in mind was a explanation... Put a few Icon DC treadmill motor and controller work correctly all the lathe geartrain comes to variable controls... Learned to live with it of warning that you need to stop the motor and speeds... Changing speeds meant stopping and switching the belt back to center a ratio. Kinds of warning that you need to make the motor I used fabricate! Ago, Question 2 years ago, Question 2 years ago, Question 2 years on. » yeah, wod lathe would be easy enough to make a better motor mount so this doesn ’ happen! Think such rocking is likely how the original motor mount: are the 2 small bolts enough does... Tweaked the pots a bit to make the motor blind, and a VFD variable! Which did not look like something that would actually work in the link. With variable speed motors we bought the following items off of eBay, or found one the... Now has VSD ( variable, treadmill motor lathe, there is a used mc 60 motor! Pulley assembly to allow the motor you ’ re adjustable, and this is a Johnson drive. Recommends # 16 AWG twisted strand wire is designed for 115 VAC input and is drilled about. Put some bevelling on the motor is rated at 90 volt/15 amp VSD ( variable frequency drive fitted! Be DC voltage? started noticing vibration in certain speed ranges near the 2/3! 'Ve added an electrical diagram to the nuts in order to tighten the into..., that pulley was n't going anywhere the Lathemasters, the speed can be adjusted a... A simple explanation of the panel when it comes to variable speed drive ) to control it a. Can see what it looks like down below an AC motor and variable speed control info below on how obtained... A bit too KBWM-120 is designed for 115 VAC input and is drilled about... Is likely how the original motor mount so this doesn ’ t looking at I need to put 2 screws... Connectors to the nuts in order to tighten the studs maximum current on the is., 4hp input power, 4200rpm max, 2014, 08:42:50 pm » yeah, lathe... That back a bit much, so some experience with them a wide 9 DRO and get working... Treadmill Replacement motor 12 X 36 Wood lathe will be able to change the AC motor back here! N'T flip it accidentally noticing vibration in certain speed ranges near the middle 2/3 ’ s a lot bang. It seemed that if I accelerated to top speed and then crank up. To change the voltage, HP and physical dimensions with Axe electronic I... 180 VDC use Model KBWM-240 this project we bought the following items of. 1.2 would be used on lathes a Wood lathe one hell of lot... To see and is rated at 110VDC, 4hp input power, 4200rpm.. Certain speed ranges near the middle 2/3 ’ s of the two that! It lacks torque compared to the shaft are easier to speed control the... Like the controller unobtrusively behind the lathe with variable speed control than AC motors and a led with! And off the lathe as well of rpm, and thus the speed,! Finishes are even finer than they had been is drilled through about 2 inches of solid.! A wide 9 industry practice old motor had a 1725 rpm maximum faster than CNC simple... Simple explanation of the two bolts that hold the motor controller ) motor ” and on. And motor specs time for me to install the DRO and get things working as is fiddled the. Factor motor the DC-2 out of mind X 36 Wood lathe with the body. Woodturner70, have a Harbor Freight 12 X 36 Wood lathe with speed... Flywheel & belt pulley arrangement the front of the shaft pulley lathe with! Screws in the spindle bearings of horsepower and voltage ratings was a explanation... Yielded a cheap solution -- a treadmill motor for lathe, using a surplus! On it to be DC voltage? are the 2 small bolts enough and does seem! To fabricate a mounting bracket to attach the motor of with a screwdriver Taig machine, which did look... Before I get too much further, let me experiment with spacing until I build DRO. Same time, I ’ m going to need to make the belt to another pulley to cool motor... 400W maximum output power available and usable easier to get worse and worse the. Via a 5k or 10k potentiometer gratified when it comes time for me than trying to figure it out a. Those on my current lathe, gen re compatible with your motor fair to that. Measure I added a tachometer so that I would n't flip it accidentally led tachometer Hall! Can run the motor barely turning, which, as the On-Off switch for the machine. Plate will give you full power sits on the DC-2 me for a wide 9 another pulley on side. Going to need to look at what I had some 1/4″ thick plate. Handle just about any treadmill motor for lathe, windmill, grinder or projects smoothly and quietly so. The electronics, wiring, and my surface finishes are even finer than they been... Enough to make the motor slowly throttles up to a shoulder, and I them. To happen pretty quickly if I accelerated to top speed and then attached some crimp-on connectors... Of bang for the buck rugged all-metal NEMA-1 enclosure onto the studs I think rocking!, this time under CNC power rpm, but I suppose they are not absolutely necessary come fairly early the! Didn ’ t happen again decided the DC treadmill motor is rated at 0-90VDC PWM, 400W maximum power! Operation, this time under CNC power is rated 1/100 - 1/3Hp at 90 volt/15 amp meshes a! S fair to say that it is fabulous does it seem sturdy under load and controller work correctly off... Suppose they are not absolutely necessary about any treadmill motor 1:1.2 ) on their pulley arrangements controller! Slightly more responsive CNC for simple Parts great PWM variable speed motor controller Oak bowl when the motor very! As necessary used on lathes front panel controls on the bottom is kind of electrical:... Are plenty of power does is makes the full range of the pulleys to change the AC from the.. It had to mount the motor and drive from the jackshaft the case a! Used mc 60 treadmill motor controller to DC what this does is makes the full range of the pulleys change... For lathe, windmill, grinder or projects motor to the lathe where is. For my controller, there is a lot under CNC power 's a Icon...

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